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Back to Basics
A Surprise
Fix to a Sticky Problem
by Emmanuel P. Papadakis*
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NDT is often called upon to do some strange things. Here is an
extremely interesting and educational story. It is about solving
a nonexistent problem! The NDT folks did it, but solving the real
problem would have been better. Basically, you have got to solve
the problem (if the requestor ever lets you know what it is).
Frank
Iddings
Tutorial Projects Editor |
Everyone
remembers a parent peeling the backing from an adhesive bandage and
applying the bandage over a scrape or a cut. This simple process has
immediate relevance to an NDT problem presented to me when I led the
NDT Research and Development Group at the Ford Manufacturing Processes
Laboratory.
The Problem
My group was informed by the Transmission Division that the friction
strips on automatic transmission bands were coming unstuck in driving
tests. The bands are about 51 mm (2 in.) wide strips of steel about
1.6 mm (0.06 in.) thick. They have small attachment brackets on both
ends. The friction strips are a sort of asbestos cardboard adhesively
bonded to the inside of the bands. The bands are like hoops on a barrel;
they go about 90% of the way around a circle of about 152 mm (6 in.)
diameter. In transmission fluid, this type of cardboard is durable and
has the proper friction against the inner steel cylinder.
The
failure mode was disbonding of the cardboard from the steel
strip.
The failure mode was disbonding of
the cardboard from the steel strip. The transmission lost torque. The
problem was posed to my NDT group as a requirement to develop a test
for adhesion of the cardboard to the steel band.
The assembly method in the factory
was to place the cardboard inside the steel band and hold it in place
with the adhesive. This adhesive was then cured and made permanent in
an oven. The adhesive, before curing, was a tacky, sticky layer on one
side of the cardboard as supplied by a vendor. The tacky layer was protected
by an impermeable layer which was peeled off just before the cardboard
was placed on the steel band. This whole operation was manual.
Searching for an Answer
The engineers brainstormed; possible causes of failure such as missing
adhesive, poor quality adhesive, unclean steel bands, improper oven
temperatures and excessive or inadequate time in the oven were considered.
What was needed from us in the NDT group was a feasible test for lack
of adhesion.
We approached the problem from the
point of view of damping of ultrasonic waves in the steel by the cardboard
when well bonded. Pulses (almost as short as impulses) from broadband
ultrasonic transducers were found to contain the spectrum of frequencies
needed to excite the bands into their fundamental thickness resonance
at the location of placement of the transducer on the outside of the
band. The resonance lasts a long time with no cardboard but is highly
damped with adhered cardboard. This difference provided a solution to
the testing problem. The areas of poor adhesion could be mapped by moving
the transducer. Research and development took about one day, as we had
all the requisite equipment in our well equipped laboratory. After that,
we investigated vendors who could provide automated systems to test
the bands. The resulting research and development was reported in
Materials Evaluation in February 1978 (Figure 1).

Figure 1
Ultrasonic system for NDT of parts using induced resonance with
damping. The enclosed region is the instrument designed for
the NDT work described in the article.
A Surprise Ending
However, before the development of the automated testing system could
get off the ground, the engineers in the Transmission Division canceled
the project. They told us that our idea was excellent but was not needed,
as they had discovered the root cause of the disbonding and rectified
it.
The cause, as it turned out, was
not faulty engineering, poor materials or failure of factory equipment.
The cause was lack of training. Everything was perfect except for one
factory employee. He was a substitute for the permanent employee who
had called in sick. The new man had been trained to place the cardboard
inside the band, but he had not been trained to peel off the protective
layer first.
Is it any wonder that the bandage
did not stick? And is it any wonder that the problem cured itself when
the sick man returned to the production line?
Our NDT Research and Development
Group, going beyond the state of the art and far ahead of the state
of the industry, had invented a useful testing method for a problem
that didn't really exist. Essentially it was a waste of time. However,
sometime, somewhere, the work should help someone.
REFERENCES
Papadakis, Emmanuel, "Ultrasonic Impulse-Induced-Resonance
Utilizing Damping for Adhesive Disbond Detection," Materials Evaluation,
Vol. 36, No. 2, February 1978, pp. 37-40.
* Quality Systems
Concepts, Inc., 379 Diem Woods Drive, New Holland, PA 17557; (717) 355-9809;
fax (717) 355-9812; <papadakis
@desupernet.net>.
Copyright ©
2001 by the American Society for Nondestructive Testing, Inc. All rights
reserved.
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